As you can see that the aircon radiator was a bit smashed up.
Unfortunately right were the boost pipe clips onto the intercooler plastic pipe, that intercooler plastic piece is cracked which renders the intercooler useless.
The radiator is in perfect shape. No coolant leakages at all and still has the original coolant.
Quite a bit of oil coming out of the boost pipe from the turbo side.It is expected since the car was on its roof and the oil just leaked from the engine to everywhere.
There's even oil in the exhaust.
Installed the battery to start it again.
This time is to find out why the engine sound like it was running on three cylinders.
The car started at the auction, although it wasn't running that great with a huge amount of smoke screen, the car did run on all four cylinders.
When the car was delivered to me I saw that a coil pack was missing and I used my spare RS4 coil pack.
Did find a faulty coil pack which I replaced.
I proceeded to rev around the 3500rpm for a while to clear out the oil out of the cylinders and exhaust.
After a short while it stopped smoking altogether and idle as it should.
Also drove it up and down the road slowly and the motor sounded fine and the DSG acting as it should, so really pleased with it. I cut my knuckles on my right hand badly since the windscreen was smashed inwards and the windscreen was only a couple of centimeters from the steering wheel.
I did find some VW invoices in the car, while I was cleaning out, and on the one invoice I see that the timing chain tensioner was replaced with the updated version, including the timing chains, guides, etc... This motor is the same one as the Golf MK6 GTI (CCZB engine code 155Kw). The CC was also subjected to that tensioner failure problem.
The CC had 116000 kms on the clock.
The motor/gearbox is dirty and needs a decent cleanup before I do any further work.
Nice and clean.
This is the back right (driver side). Notice the tyre rubber wrapped around the axle.
Not really sure what happened to the car, but looks like some sort of a blowout, lost control, went down a steep embankment and once reached at the bottom it must have flipped onto the roof from the front. There's no side damages whatsoever, so it did not roll either the left or right side onto the roof.
The tyre rubber that I pulled from the back axle.
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