At the time it had this oscillating AFR issue. Which has been difficult to nail down. Not the software as it's pretty close to Lito's Golf. There was an inline pump which under WOT seemed unable to supply enough pressure. This was confirmed with a fuel pressure gauge. Although the pressure was rising under boost, it wasn't maintaining 4 BAR above manifold pressure. So the ECU was trying to compensate for this and couldn't.
That pump was removed and then it was run with a new intank pump, which still seemed to under perform under WOT but the pressure was following boost properly. A couple of weeks back the fuel filter was replaced again, the one coming out had been in for only a few hundred ks. Anyway, it seemed much better on the road but still need to log it to see if the drivers seat impression is true.
Fingers crossed next time Richard is back home we can finally nail it.
Gavin
Bookmarks