i was getting real bad surging after my APR tune the boost would go up and down crazy was over boosting to 22psi then dropping to 15psi it was the N75 valve trying to keep up and cut boost most of it when away once i fittest my FMIC then i put a MBC inline with my N75 valve to slow the air to the N75 valve and it runs very smooth now and comes on boost faster.
Last edited by HAR80N; 12-09-2015 at 10:21 AM.
My Beast: 06 Polo GTI~White~Milltec CBE~APR V2 Tune~SuperPro Bushes~WhiteLine FSB~Phenolic Spacer
2nd Beast: 02 Audi S3~Stock
Bookmarks